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Running and Racing Reliably Part II: Continuing At The Bottom

Assembly tips, tweaks and techniques for a properly built 455 HO
By Thomas A. Demauro
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Here are our TRW pistons installed, viewed from the top side. The block to head mating surface of this block was not decked because it was true, according Taylor. Performing the procedure would have wasted metal and money unnecessarily. We'll explain the numbers on the deck later.
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A lower dipstick tube and the windage tray are test fitted next. The lower tube is inserted into the through-the-block tube and the tray is installed with the tube passing through it. The lower tube is marked for depth and removed to check to make sure that it slides into the through-the-block tube far enough. About one inch is acceptable. Rarely will the windage tray just drop into place. More times than not, the tray will not line up with the bolt holes in the main caps to secure it because of misalignment of the tube. Many builders will put pressure on the tray to line up the holes and just bolt it down. The tension on the tray when installed is one of the main reasons that so many trays crack. So Jim uses a chrome-moly pushrod as a tool to maneuver the lower tube into the proper position.
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Then the tray is installed again. The process is repeated until the tray mounts perfectly over the four bolt holes with no tension on it. The tray usually cracks right where the tube goes through. Note that we are using a 455 tray. There is a "5" barely visible on the top in this photo. The engine should be rotated after the tray is installed to ensure that there's no interference. The bolts get Loctite.
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Some builders will tack weld the lower tube to the through-the-block tube to ensure it doesn't fall out during operation. Taylor prefers to stake the tubes. "Welding is little extreme when staking does the job," he told us.
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There is some custom work done to fit the pan for a leak-free seal at the rear. Here, Jim's apprentice builder Mark Erney marks the rear main cap through the slots in the pan to determine proper positioning of the cork seal.
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This engine will use a two-slot one-hole oil pan, which would normally require a rubber gasket, because that's the design the aftermarket has adopted. The other two styles (see Panning for a Good Seal before continuing) have gotten very scarce. A smooth rear main cap is also used. However, Jim will still employ a cork gasket because he feels that it seals better than rubber. The seal is installed dead center of the pan rail on the cap, a position provided by the earlier measurement. Permatex Silicone Adhesive Sealant (clear) is built up on either side of the cork to create dams to retain it. According to Jim, "It looks ugly but it works very well!" This setup is left to cure overnight.
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While the rear pan seal cures we will turn our attention to the 224-113R Sealed Power oil pump that will provide the needed pressure and volume to feed the 455 HO. The pump is completely disassembled to double-check its components. Shown (from left to right) are a feeler gauge to check clearance between the gears and the pump cover, the gears, a check-ball, the plug to retain the check-ball and relief spring, the extra-thick pump cover to ward off flex, the cover retaining screws and the relief spring.
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It's important to examine the check-ball seat (inside the upper hole) to ensure that it's machined concentric and its width is constant. The check-ball seat is machined in after casting. If core shift is severe or a material void exists during casting, it will effect the seat. This is very rare but it does happen, according to Jim. A telltale sign is low oil pressure at idle due to oil leaking past the check-ball and seat but normal pressure at higher rpm since the check ball is off the seat at this point. Here you can see that the casting process did in fact encroach on the check ball seat but the amount is not enough to cause concern in this street engine. This pump will be fine to use.
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Though this is a Sealed Power pump, Jim prefers a Melling pickup in street engines. The Melling piece on the left has a finer mesh screen that will filter finer particles in this street engine. Conversely, the Sealed Power pickup (above) has larger openings in the screen, better for racing because there's less pumping restriction than with the Melling unit.
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Mark taps the pickup to press its tube into the pump and align the screen with the notch in the pump body. This installation tool is homemade and designed to press in the pickup without damaging the tube.
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The pump was installed with the bolts finger tight in the block because the factory bolt shoulders are not wide enough for interference fit through the pump body. Using this to his advantage, Jim positions the pump to provide a straight shot from the gear rotor in the pump to the bottom of the distributor. The bolts are tightened to 30 lbs.-ft. With the pump installed, you can see the Nunzi pump drive. Note that the collar completely surrounds the tang on the pump unlike the factory piece and other aftermarket replacements. Also, the Nunzi piece is made from better materials than typical replacement drives.
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Here is the completed bottom end prior to mounting the oil pan.
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To determine whether the screen is positioned with the correct distance from the floor of the oil pan, a measurement is taken using a straight edge across the pickup from both sides of the pan rail. The two measurements are averaged and equal seven inches.
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The pan depth in the pickup area is measured from the pan rail to the pan floor resulting in 7.25 inches. So the clearance between the screen of the pickup and the bottom of the pan is .25-inch--just what it should be. But the pan can't be installed yet. To find out why, stay tuned for the next issue when we wrap this motor up.
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Panning for a Good Seal Pontiac V8 rear oil pan sealing systems were changed a few times between 1955 and 1981. This sidebar illustrates the difference between the types of rear pan seals and the two different rear main caps that accepted them.--TD The earliest is this pan, which features no holes and has a stamped lip to retain a cork seal. Taylor considers this the best design.
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A rear main cap like this one, that has a groove to hold the cork seal in place, was employed with the early style oil pan.
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The next design, that debuted in about 1974, has a flat surface with no stamped lip but has two slots and a hole to retain a single lipped rubber gasket, as shown. This is considered the worst design by Taylor because the gasket can easily push out due to the fact that the retaining tabs on it are so far apart. The result is leaks.
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Pontiac must have concurred with Taylor's findings since this design came later from mid '70s to date. It has 5 slots to retain a double-lipped rubber gasket and greatly reduces the gasket's tendency to push out (when clamped) and leak.
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Both of the rubber gasket-type pans are used with a rear main cap that has no provision for the old cork
High Performance Pontiac Engine Buildup Worksheet
Engine Displacement:462 cubic inches
Projected horsepower:425
Projected torque:510
Bore/Stroke:4.180/4.210
Block/Crank combo:455 HO
Bottom End
Block description:455 HO service replacement
Year:1972
Preparation:Hot tanked, magnafluxed,align bore checked, bored and honed .030over with a torque plate, deck was checked,it was okay
Deck Height:10.225 inches
Crank:1972 Nodular-iron
Preparation:Hot tanked, magnafluxed,index checked, wire brushed oil feed holes, cut .010 on the mains and rods, radiusedoil holes, checked pilot bushing area if amanual trans car, checked snout to ensureproper balancer fit
Balancer:New Delco
Type:Stock replacement, degreedby Jim to show 16° and 36° BTDC
Rods:1957 Forged steel
Rod length:6.625 inches stock
Preparation:Vacuum heat-treated,balanced, checked for straightness and sized
Bearings:Clevite 77
Preparation:Clean and inspect
Pistons, brand, type:TRW forged aluminum
Preparation:Balanced, cut groove for lockfor full-floating pins
Piston to deck height:.015
Piston pins:TRW tool steel, full-floating
Method used to retain piston pins in pistons:Snap ring locks
Rings:Sealed-Power, moly top, cast-ironsecond (part No. E300K)
Preparation:Checked each in bore for properend gap, file fit as needed to get it deburred
Rod bolts or studs/head boltsor studs, brand:ARP
Oiling System
Windage tray:Factory full tray
Oil pan:Milodon
Oil pump:Sealed-Power with Melling pickup
Heads
Casting number:7F6
Chamber open/closed:Open
Head mods:Mild intake porting, portmatch, blend the bowls
Combustion chamber volume:103 ccs
Maximum flow at 28 inches of water:Intake--235 cfm at .500
Exhaust--180 cfm at .500
Compression ratio:9:1
Valves:Ferrea stainless steel
Intake size:2.11, swirl polished, 5.100 long
Exhaust size:1.77, swirl polished, 5.100 long
Angles used in valve job:15°, 30° seat, 65°
Retainers:Crane
Keepers:Crane 7°
Valve guides:K-Line bronze liners, honed to size
Valve seals:Teflon on intake positive seal,exhaust new Viton positive seal
Rocker studs:7/16 GM HD
Rocker arms:Comp Cams roller tip
Rocker arm ratio:1.52:1
Pushrods, brand:Crane Energizer,delivered hardened for guide plates
Diameter:5/16
Length:Stock
Cam
Brand:Crane Hydraulic
Duration at .050:228° I/E
Lift:.485 I/E
Lobe separation angle:112°
Installed position:110°
Lifters:Crane hydraulic
Valve springs:Crane, dual with a damper
Seat pressure:110 lbs.
Open pressure:260 lbs.
Timing chain:Rollmaster, double roller,.250 seamless
Induction
Carb:Rebuilt 1973 750 cfm Q-jet 455
Primary jets:73 or 74
Secondary metering rods:.052 or .054
Intake manifold:Edelbrock Performer intakefor a Trans Am with low hood clearance.
Mods:Gasket match, won't get perfect portalignment but that's okay according to Taylor.
Ignition
Distributor:GM HEI, recurved and rebuiltby Larry Rowe
Coil:Stock
Wires, brand, type:Stock
Total Timing:34° all in by 3200 rpm
Initial advance:16°
Mechanical advance:18°
Vacuum advance:None
Exhaust
Stock HO manifolds 
Gaskets
Brand, type:Fel-Pro


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